This week I worked on getting the frame painted so I can start putting things back together.
I just used spray bombs for the primer so I could just prime what I got sanded out each night.
Since I don't expect to have this paint job on the frame for more than a year or 2, I am using Rustoleum Rust Stop for the top coat. I got the paint for $6.99 a quart on sale. I made my own custom color by mixing Aluminum with Gloss Black in a 50/50 mix. I'd probably mix it with more black than aluminum if I did it again as it looked darker in the can than it does sprayed out.
Primed out ready for the top coat.
Top coat applied today. The biggest drawback to the Rustoleum is how long it take to dry, it's super slow and today's high of 44 degrees today didn't help. I did run the furnace in the shop to warm it up to about 60 inside before I started painting, but my only method of ventilation is to open the garage door, so it doesn't stay that warm when it's 44 or less outside. It does spray out pretty smooth though, but you have to be careful not to get runs with the slow dry time.
My side project of the week was the frame stud for the clutch cross shaft. I ordered one made by Danchuck from Summit Racing but they only had the 56 to 57 one. I was ordering some other parts from Summit anyway so I figured I would just have to modify it to save the shipping cost to buy the right one from elsewhere.
Turns out the 56 to 57 frame stud is an 1/8" bigger diameter and has a longer shank than the 55 frame stud. To turn it down to the right dia. for my 55, I chucked it into my poor man's lathe/drill press. I clamped a piece of stock in the drill press vice to use as a tool rest to file it down to the right dia. I used a coarse file first and just kept checking it with a caliper until it was close and finished up with a finer file.
To shorten up the shank I wrapped the stud threads with making tape so they wouldn't get damaged in the chuck. Then I set the tool rest so I could use the edge of a flat bastard file as a parting tool.
Then is was just a matte of moving the tool rest up to take down the rest of the shank to size. It took a couple of steps to get the whole thing down to size.
Here is the finished stud modified for use in a 55 Chevy. I tried to cut threads on the new shank but couldn't hold it tight enough without risking damage to the stud ball so I'll just have to use a few extra washers when I bolt it on. I should have cut down the shank first then cut new threads before turning down the stud but I didn't figure out the shank was to long until after I had the ball end finished.
Tomorrow I will be working on priming and painting the Corvette K-member, trans cross member and upper shock mounts so those can get bolted back in the frame. It's supposed to be 55 degrees so hopefully paint will dry a little faster.
Brian